Eon NRG announces successful gas well recompletion
Tuesday, Apr 17, 2018
Eon NRG Limited advises production update on the gas well recompletion carried out at the Silvertip Field.

The 35-28 Gas well recompletion:

The 35-28F well was recompleted in an untested sand lobe within the Meeteetse Formation. This well was originally drilled to the Frontier Formation where it produced natural gas and oil. The well recompletion has produced in excess of 30,000 Mcf of gas since it was brought back into production on February 8, 2018. The 60-Day IP average daily production rate was 487 MCF/D and production for the last 30 days has averaged 650 MCF/D. A 16/64" choke is in place and has a stabilized flowing casing pressure of 390 PSI.

The recompletion cost was $22,000 as it was carried out utilizing an existing wellbore and the company's inhouse expertise. This recompletion has generated net revenue (after royalties and production tax) of more than $60,000 in the first 60 days of operation. The capital cost of the recompletion was paid out in less than 30 days.

The Company is evaluating the potential of further recompletions in the field on wells that may have similar formation characteristics to the 35-28 well.

For more information, please visit: http://www.eonnrg.com

For additional information on this project, please visit our ProjectsOGP database
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